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Get Off My Lawn

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About Get Off My Lawn

  • Birthday 06/01/1965

Personal Information

  • Name
    Geoff Dirks

location

  • Location
    Monroe, WA, United States

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  • City
    Monroe

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  • State/Province
    WA

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  • Home Country
    United States

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  • Bike Year and Model
    87 Venture Royale

Occupation

  • Occupation
    Automation Technician

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  1. And the problem is back. Ok time for a dive into the deep end and do a carb rebuild. None of the shops are interested or taking new work, as they're all backlogged. Of course, it's Spring. I've got to dig through the forums now for a carb rebuild how to or videos. Suggestions are welcomed
  2. Resolved the carb4 float bowl puke problem. I flushed/drained the float bowls a couple times, but that didn't resolve it. I pulled the carbs, sprayed and blew out the main and pilot. Then the fun of putting the bank and throttle cables back. Fired up right away and although it's running a bit rich, she's alive. Worth replacing the (new but fouled) plugs?
  3. Revisiting this. It's been a strange few months hasn't it? I was declared 'essential' and have been super busy working non-stop, almost never have time to work on my bike. I finally started working on it, and cleared out the old oil. What a maroon. I drained the oil from the filter and not the drain plug. I can't believe I was that stupid. That got all the old oil out, and bonus: I discovered the previous owner never had a plate washer between the spring and the filter O-ring. Of course, that chewed up the O-ring pretty well. New filter, with plate washer, new oil, proper amount, etc and.... the same carb is puking gas again. Unless someone has a better idea, I'll be pulling the carbs and cleaning them out again. I'll try some carb cleaner first.
  4. Forgot to update the thread. I resolved the sticking float on that carb, without removing the very tightly pressed in float valve seat. I thought I'd put her all back together and see if it worked. I made up an external rig to see if the float bowls filled and the float shut off the valve. It worked. Nothing running out the float overflow. Reinstalled the carbs, fought with the throttle cable, drained the tank as much as possible, refilled with fresh premium zero ethanol (thanks to pure-gas.org), and pressed the magic button. Started up right away, and ran ok with some hesitation. almost feeling like there's a cylinder not effectively firing. I warmed her up and did an oil/filter change and I think I overfilled using 4 full quarts, but the owner's manual and shop manual both said 3.8L(4qts). Now she smokes like an old 50s femme fatale and fouled the plugs after just 5 or 10 minutes running up on the centerstand. It was not smoking before I cleaned the carbs and replaced the float needle on the one carb. Ideas?
  5. I like that idea. Heh. Yeah, from the inside out. I was just at my local shop, and they asked the 'old' tech who started in the 80s (OLD?!?!?) He said he's never had to remove one of those, and recommended some 800grit to clean out the upper throat (NOT touching the bevel seat) I'll try that. Before I put them back on, I'll rig up a test. to see if the float needle actually seats. It's only one carb giving me grief, and I've ordered the cap and O-ring anyway. It's raining again so I'm not missing any riding anyway Thanks again.
  6. HOw hard do you have to hit the punch to get that float seat out? I've given it a few good taps taps, but it's not budging. On my way to my local shop to pick some brains.
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